Tag Archives: fuel

November/December 2004 – Firewall sundries

An odd fall, this last one. Sometimes it was as warm as summer, and then, before you get too used to the nice weather, in popped a cold spell for a visit. I still have some paint touch up to do before I can turn to the final buffing and shining, but I’ll need some sustained warmth before I can swing the paint sprayer again. Now that it’s almost the turn of the year, warmth might wait ’til spring to come back.

So, over the past couple of months, I’ve done various things, mainly on the areas of the car forward of the firewall (“front bulkhead”), but also some on the interior. I’ve devoted a page to the specifics: the firewall section (this page), the front suspension, the steering setup, the pedal and master cylinder asssemblies and the rest. “The rest” means the left over of what I did, not the rest of the car, unfortunately. It includes beginning installation of sound dampener/insulation on the interior, shipping some chrome off to be redone, and beginning work on breakdown of the IRS.

Firewall Sundries

The firewall is a place for lots of individual parts, so as you go about refinishing and reinstalling them you do get the feeling that you are really moving along. The nice thing about the firewall work is that you can also tackle a complete piece in an evening or two, making for a satisfying pace. When I compare the firewall clutter on my truck (a ten-year-old Ford F-150) with the minimal stuff on the Jag firewall, the difference is amazing. There really isn’t much on the old Jag, and what was placed there seems to me to have a certain ornamental flair. (Perhaps that is a bit of bias impinging on judgment.) That simplicity comes in part from the fact that the firewall had to serve both right-hand and left-hand drive configurations. So there are many parts that are placed in a somewhat mirrored fashion, not exactly mirrored of course. This means that something like the blanking plates for the pedal assembly are required on the Jag, whereas I don’t think my pickup has anything like those. And since they’re on the Jag, they could be adorned with cadmium plate. And since the configurations are mirrored, the firewall always has some area more or less unused opposite the used space, though individual sections of the firewall are also set up so that they can accept different parts.

The first thing I took on was the wiper motor. It’s basically a steel sheel surrounding the rotor and armature with pot metal caps. A gear assembly comes off the top of the motor and contains a large nylon gear driven by a brass worm gear off the motor. The motor itself is straightforward, but the controls are a little formidable because of the requirement that the wipers “back off” and go back into their off position once the wipers are turned off. This means reversing the motor to set the wipers into their resting place.

I was a dolt and tried to make the motor move by touching wires with a six-volt battery charger. There wasn’t anything that moved, and when I thought that perhaps this was a stupid thing to do (after a couple of touches to no effect), I gave up. I asked about ways of testing the motor on the Jag-lovers forum, but apparently there’s not much to do until the switches and wires are correctly installed. I was warned about messing with battery charges and delicate wiring, though!

Putting the motor into visible order was a matter of dismantling the pieces and cleaning them up. The steel motor housing is painted a hammered silver/grey. I used a multipurpose grease on the gears. They had been greased before, and the grease had firmed up quite a bit. It wasn’t hard or rubbery, but it was old and stiff. Installation of the motor was a matter of fitting the wiper arm and sliding it into the inner part of the firewall and bolting the mounting plate. Now I can look at it and hope it will work.

The windshield washer jar and pump were original, as was the mounting bracket that attaches them to the firewall. The washer pump lacked a part that apparently sits below fluid level and is driven by the small motor mounted on the jar lid. This meant, of course, that the pump was functionally worthless, even though it looked good after cleanup and a spray of satin black paint. New washer pumps are available, but they don’t look like the old one I have, as far as I can tell. I decided to mount a “universal” washer pump in the area inside the firewall behind the washer fluid jar, and let it use the existing lid and tubing to draw fluid from the jar. It’ll be invisible, and it should work to pump fluid. Although I will hook up the contacts on the old pump, they won’t be connected. Instead, the real wiring will go to the new and hidden pump.

New rubber tubing was fitted. I got it from McMaster-Carr, a place that amazes me continuously. I also installed the first rubber grommet in the firewall for the washer tubing. This grommet came from the body seal and rubber kit that is offered by Classic Jaguar. I look forward to installing the rest of the rubber parts!

The mounting bracket was a bit of a job. The rubber guard on the side bars (see the closeup picture of the restored part) completely rotted and had turned into little more than a sticky goo. More rubber had deteriorated at the base of the bracket. I’m not exactly sure why it behaved this way, since it appeared to have been dissolved in some fashion. By solvents in the washer fluid, perhaps? At any rate, that had to be completely removed. After I stripped the paint on the remaining parts, I repainted gloss black, leaving the side bars unpainted. I decided to try reapplying the rubber coating with Plasti Dip, a product that is used to give tools a rubber-like grip on their handles. You usually dip parts into the product, but I brushed it on the bars. It took several coats to build up sufficiently, but the end product looks quite good. The Plasti Dip looks like it will be quite durable, too. I have loads of the stuff left.

The fuel filter bowl and the bonnet latch assemblies also went on after thorough cleaning. I’ll be removing the fuel filter bowl to install the car number plate. I’m a little disappointed wth the reproduction of the car number plate. It evokes the original, but it doesn’t come too near duplicating it. The past couple of days I’ve been toying with the idea of doing my own (and more true) number plate. It seems that the people who did the reproductions could have been more scrupulous.

October/November 2004 – Gas tank

Gas tank cleanup and sealing

The gas tank had waited in the chicken coop for two years. That was long enough to take on a couple of boarders — mice who built a nice soft nest behind an inside baffle. In spite of the fact that the gas tank was bone dry from the first day we got the car, I know that mice hadn’t invaded until we took possession. The nest I pulled out piece by piece and sucked out with my shop vacuum was made of our brand of paper towel and a cotton swab or two that had been lying around. I had to use some wire to fish out the little bits. Time to set more traps, I guess.

I glanced inside the tank when we put it into storage, and I recall thinking that it was pretty rusty, though I was also happy that the tank was completely empty and had been for some time. Perhaps it is a matter of perspective now, but looking at it after two years of repairing other (worse?) rust made it seem a little better. The rust inside was scary nonetheless. There was a welded repair that had been covered with blue silicone sealer. I recall the previous owner pointing to some blue stuff and saying “Kreem?” but I have to admit that “Kreem” didn’t make much sense to me then. Now I know it is a type of gas tank sealer. Our closer look inside the tank showed us that the tank had never before been treated with a gas tank sealer. That fact simplified our work, since we wouldn’t have to remove a previous sealer to apply our own.

The underside of the tank, on the corner nearest the threaded hole for the fuel sump, had been repaired by cutting out a rusted area and patching it. The rest of the tank wall was unmolested and solid. The rust repair was probably done at the same time as the “repair” of the fuel sump hole on the trunk floor that we redid. This area of the E-type is commonly rusted, I’ve heard. It can collect water, since it is in close proximity to a hole fairly near the pavement and since Jaguar apparently used jute pads to soundproof. The jute pads were situated between the gas tank and the floor of the trunk. Unfortunately, they soaked up moisture and eventually promoted rust.

Bottom line: We didn’t need to do rust damage repair, though sealing and removal of lesser rust deposits were still needed.

I decided to use POR-15’s “US Standard Fuel Tank Sealer” kit. I’d read positive reviews, and I’ve been overall happy with other POR-15 products I’ve used. I know that the rust protection coating is mighty tough stuff, and I figured the sealer would be tough, too. Also, I was attracted by the simplicity of buying a kit that included everything I’d need. Cost was in line with what I expected: $50-$75. My kit arrived with two quarts of “Marine Clean” detergent, a quart of “Metal Ready” rust converter and metal etcher, a quart of sealer, and a large-ish container of fuel treatment, that I won’t use until I actually put gas into the tank. A single letter-sized sheet contains all of the instructions. In short, you clean the tank thoroughly, convert any remaining rust and etch the steel, and then coat with the sealer. (See the sidebar for all the details of our sealing job.)

Since I wanted to make the most out of the detergent that came from POR-15, I decided to do a pre-cleaning of the inside of the tank. There was no sense in pouring in the special detergent to do what regular old “industrial strength” degreaser-detergent would do. To that end, I used a 1:1 dilution of Kirkland brand (yes, it came from Costco) “industrial/commercial” degreaser-detergent. This stuff is colored a flourescent-like green. I’ve used it to degrease parts and I’ve even used it — with spotty results — to clean items that were to be zinc plated. It has worked very well to remove grits and greasy deposits. I used the regular degreaser in the same manner that the POR-15 folks recommended using their “Marine Clean” detergent. The first cleaning really took out a lot of junk, both loose chunks of grit and flaked rust and dissolved goo. The detergent mix came out looking like eight-hour old espresso. After a clean water rinse, I redid it. The second batch of detergent came out signficantly more clean, but still definitely brown. The third batch came out virtually the same color as it went in (see the left half of the comparison picture in the sidebar), so I figured that the detergent had done as much as it could.

At that point, I began using the “Marine Clean.” Now, “Marine Clean” is a clear liquid, and the POR-15 people claim that it dissolves varnishes and residues that result from oxidizing fuels. Apparently this works in gas lines as well as gas tanks. I actually wasn’t expecting the “Marine Clean” to get as much out of the tank as it in fact did, since I’d already cleaned the tank with some also pretty tough detergent. That “Marine Clean” really works — the first 1:1 dilution came out significantly brown, indicating it was at least dissolving what my other detergent couldn’t. The second dilution also came out somewhat brown. One thing that was a bit unsual was that the instructions suggested that there was a third application of the “Marine Clean,” but my kit contained two quarts of the stuff. I figured that the POR-15 people decided that three was overkill and two would suffice.

The test of the relative strength of a “industrial” degreaser-detergent and the POR-15 “Marine Clean” detergent was really the only surprise in the process of sealing the gas tank. The rest of the process went without much to note.

After the inside was sealed, I painted the outside of the tank. I did decide to mask the areas where the fuel pump and the fuel level sensor attach as well as the threads for the fuel sump. These now are clean metal. I am thinking about installing a different (more dependable?) fuel pump, though I’m not sure what type, submersible or not. That is a question I do not need to answer right now, however.

The gas tank looks nice. I’ll have to keep more rodent boarders from moving in!


Gas tank treatment, step-by-step using POR-15 Fuel Tank Sealer Kit


Pretty scary, I thought, when I first took a look at the inside of the gas tank. This area is the welded repair that must have been associated with the rusted out trunk. I think that the rusted out trunk floor became a problem when gas began to leak. The area immediately adjacent to the welded repair on the tank exterior had some pitting as well.

The instructions for the tank kit said to clean the tank with the “Marine Clean” detergent, diluted 1:1. I decided to use some regular old “industrial degreaser-detergent” (purchased from Costco) to do the initial cleaning. This entailed sloshing around a 1:1 mixture of water and degreaser. I did this three times, and I let the detergent soak for about an hour in the tank. The first time the mixture came out a coffee-colored liquid. After a clean water rinse and another Costco-brand slosh, the detergent had done as much as it could. It came out almost completely the color it went in. The picture above shows the results on the interior — there were some results but the best was yet to come.

The picture shows the last Costco-brand detergent and the first “Marine Clean” detergent mix. It’s pretty obvious that the Costco detergent had done its best. And the “Marine Clean” — which went in completely colorless — came out quite brown. The “Marine Clean” detergent is claimed to remove fuel residues and varnishes that appear in fuel tanks and fuel lines. I was skeptical, but I was pleasantly surprised by the result, especially after I had cleaned up as best as I could with other detergent.

This shows the tank floor after two applications of the “Marine Clean” detergent. Although the instructions said that the final detergent soaking would pour out almost clean, that was not my experience. That second soak came out brownish, too. I’m assuming this second application was adequate, since a third quart of “Marine Clean” did not come in my kit, although the instructions mention a third application of the diluted detergent. What is shown here really amounts to a thin coating of rust. I could easily rub it off with my fingertips.

After the inside is free of greases, oils, and varnish, the rust is converted with a product called “Metal Ready.” Basically, this converts iron oxide rust and etches the metal surface. This left (or, perhaps more accurately, replaced) the rust film with a grey film that came off just as easily as the rust. This picture shows the treated surface after it had been rinsed with clean water. The surface came quite clean, since you can see the brazed welds quite easily and the steel looks like steel.

An old hair dryer served as the forced air source. It was perfect, since I just shoved it in a hole and turned it on. For the most part, I kept the dryer running without using the heater. Hot air went in about three hours all told, and it definitely heated the tank. Overall, I ran the hair dryer about ten hours. Completely drying the inside of the tank is very important, and the kit instructions especially stress this. The tank sealer will not adhere to a wet or moist tank wall.

The POR-15 kit comes with a quart of fuel tank sealer, which looks to me to be the same stuff as POR-15 metal coating. Stinks the same, at least, and it looks pretty much the same, too. We duct taped the openings on the gas tank, poured the sealer into the very dry tank, and rotated it to make sure that the coating covered the entire interior surface. After that, we poured the excess out — about a pint remained. The kit instructions said to leave the can open, so that it wouldn’t explode (!), and that does make me think that the sealer is somehow different from POR-15 metal coatings, since those are resealable, at least for short term.

The inside of the tank now looks like this. The POR-15 instructions say that you can repair larger holes with a fabric-like product and POR-15 sealer applied to the outside of the tank over the holes. Thank goodness we won’t need to do that kind of thing!